ILLINOIS POLLUTION CONTROL BOARD
    May 3, 1972
    ENVIRONMENTAL PROTECTION AGENCY
    #70—34
    v.
    GRANITE CITY STEEL
    COMPANY
    ENVIRONMENTAL PROTECTION AGENCY, BY WILLIAM J, SCOTT, ATTORNEY GENERAL,
    STATE OF ILLINOIS, BY HERBERT CAPLAN AND JOHN W. LESKEBA, ASSISTANT
    ATTORNEY GENERALS; AND THOMAS C. SCHUENEMAN, DEPUTY DIRECTOR AND
    FRED PRILLAMAN, BUREAU OF LEGAL SERVICES, ENVIRONMENTAL PROTECTION AGENCY;
    GRANITE CITY STEEL COMPANY BY JENNER AND BLOCK, THOMAS S. SULLIVAN
    AND LEAH HAMILTON; LEUDERS, ROBERTSON & KONZEN, BY RANDALL E. ROBERTSON
    OPINION OF THE BOARD (BY MR. LAWTON):
    This Opinion is pursuant
    to Order of the Board entered in this
    cause on April 25, 1972 approving a Stipulation and Agreement between
    the parties disposing of the complaint and providing for the installa-
    tion of air pollution abatement equipment and the adoption of operation-
    al procedures designed to control the emission of particulate matter
    resulting from the operation of an integrated steel mill operated
    by the Granite City Steel Company located in Granite City, Illinois.
    Complaint (later amended) was filed against Granite City Steel
    Company (“The Company”) by the Environmental Protection Agency (“The
    Agency1’) on November 9, 1970, asserting that from June 1, 1967 to
    the date of the filing of the amended complaint, Granite City Steel
    Company had operated its by-product coke plant, quenching tower,
    sintering plant, basic oxygen furnaces, blooming plant, rolling mill
    and blast furnaces in violation of the Rules and Regulations Governing
    the Control of Air Pollution with particular respect to particulate
    emissions, Section 3 of the Air Pollution Control Act (Ill. Rev. Stat.,
    Ch. 111—1/2, Par. 240.3 (1969) and Sections 9(a) and 9(b) o~the En-
    vironmental Protection Act, (Ill. Rev. Stat., Ch. 111—1/2, Par. 1009(a)
    and (b) (1970).
    Answer was filed by the Company. Extensive discovery proceedings,
    by way of depositions and Interrogatories, were pursued by both sides
    and a series of pre-trial conferences was conducted by the Hearing
    Officer to resolve various issues raised with respect to interroga—
    tories and to establish procedures for the conduct of the hearing. A
    motion to dismiss the complaint was filed by the Company alleging
    constitutional and statutory grounds. The Clean Air Coordinating Coun-
    cil and the League of Women Voters of Illinois were permitted to inter—
    4
    457

    vene for the limited purpose of challenging the Company’s motion
    to dismiss. By Opinion and Order of the Board entered on March 17,
    1971, the Company’s Motion to Dismiss was denied.
    Subsequent thereto, approximately thirty hearings were conducted
    in the trial of the cause, principally in Granite City, with several
    hearings in Chicago beginning in May and suspending in September,
    1971. The Agency’s case in chief in support of the complaint was
    substantially completed but
    was
    interrupted in order to permit the
    testimony of Dr. Werner Eisenhut, a witness introduced on behalf of
    the Company from Essen, Germany, who, because of personal problems
    was permitted by agreement to testify out of sequence. The Agency’s
    presentation, to the extent completed, consisted principally of testi-
    mony of various Agency employees, who testified as to their observations
    with respect to particulate emissions and Ringelmann violations eminating
    from the various facilities of the Company alleged to be in violation.
    A substantial number of photographs were offered into evidence.
    Officials of the Granite City Air Pollution Control Board and
    several neighbors in the vi~nityof the coke ovens and basic oxygen
    furnace also testified on behalf of the Agency to the alleged impact
    on the community resulting from the operation o~ these facilities.
    Several officials of Granite City Steel Company were called by the
    Agency as adverse witnesses. The testimony of Dr. Eisenhut, on be-
    half of the Company, related to the state of the arts of various abate-
    ment facilities being employed throughout the world in regard to charging,
    pushing and quenching inherent in the coking operation, which aspects
    of his testimony will be considered in more detail below.
    In the fall of 1971, both sides represented to the Hearing
    Officer that they were in the process of formulating a settlement
    proposal pursuant to the terms of which the Company’s steel—making
    processes would be brought into ccmpiiance with the relevant statutory
    and regulatory provisions relating to air pollution. Request was made
    that the hearings be suspended so that the prospect of settlement could
    be more fully explored.
    A proposed stipulation and agreement was thereafter submitted
    to the Board, which, because of certain procedural aspects was not
    deemed acceptable, These objections were later removed by modifica-
    tion of the agreement which, as modified, was resubmitted ~o the Board.
    The Board directed the Hearing Officer to resume public hearings pursuant
    to Pollution Control Board Procedural Rule 333. Two additional days of
    hearings were conducted in Granite City limited to the elements of the
    proposed stipulation and agreement. After consideration of the tran-
    scripts and exhibits the Board, on April 25, 1972, entered its order
    approving and adopting the stipulation of settlement as the Order of
    the Board. The principal features of the Agreement will be considered
    below:
    4 —
    458

    The Company agrees to establish a scholarship fund payable
    to the University of Illinois for studies related to environmental
    quality, through undergraduate and graduate college level disciplines,
    in the amount of $150,000.00, to be administered by the President
    of the University of Illinois; $50,000.00 is to be paid within seven
    days of the entry of the Order and an additional $50,000.00 on or
    before January 2, 1973 and the balance by July 1, 1973.
    The Company agrees to install and operate an AISI coke oven
    charging air quality control system on or before thirty months from
    the date of the Order, which installation is anticipated to cost
    approximately $2,150,000. This facility is represented by various
    witnesses who constitute the most advanced state of th~arts in the field
    of coke oven charging operations. Dr. Eisenhut testif~~that
    .xperimentation was presently being conducted with five t~es of
    pollution control devices used in the coke charging proces~. They
    were, first, Larry cars with wet scrubbers; second, gravity ea~rs;
    third, Larry cars with steam Venturi scrubbers; fourth, the Re~er
    Conveyor; and fifth, pipe line charging (R.3444—3491), It was h~e
    opinion that for ada~’tatiOn to existing coking faci1ities,nth~gráv~tv
    car with the AISI modifications would represent the best technology
    available and would abate charging emissions by 96 to 98. Use of
    the gravity car would preclude the need for pre-ignitiori of charging
    gasses required when wet scrubbers were utilized, and would not
    possess the additional weight that has made the addition of other
    abatement devices on the car unsuitable, The gravity car would not
    employ a scrubber but is designed in a manner so that as the coal is
    charged from the car through the charging holes, the gases are sucked
    into a collecting main through the employment of steam vapor jets
    and at the same time, a temporary seal is formed at the point of en-
    trance preventing the escape of gas at this location. The American
    car designed for use by the Company is an advanced version of the
    German car with improved closure mechanism and valving. Automatic
    lid-lifting devices are employed precluding the need for moving of
    the car before the lids are replaced. Plans and specifications for the
    AISI coal charging car are included in the record as Exhibits 84, 85
    and 86. In addition, a leveling bar is utilized which prevents
    emissions from the leveling door. The cabin of the operator is
    air-conditioned. The entire operation is automatic, eliminating the
    need for any manual labor. Donald Cairns on behalf of the Company,
    described the operation as follows: (April 12, 1972, R.39).
    “We have automatic onespot lidding of the ovens,
    that is the car comes up to the oven to be charged
    with the drop sleeves in place, the lids are removed
    magnetically, the drop sleeves fall into place, the
    coal is charged into the oven, and then any off gases
    of smoke which might evolve during charging are sucked
    over into the by—product main through steam, improved
    steam aspiration at the stand pipe. Then the charging
    sleeve is withdrawn, and the charging hole lid is replaced
    magnetically with this control.”
    4
    459

    The agreement provides for improved work rules with respect
    to the self—sealing doors on the coke ovens. These doors are self—
    closing and according to Dr. Eisenhut (R. 3515-19) there are
    ilO
    doors
    presently available that are better able to prevent emissions during
    coking. The knife-edged self-sealing doors appear superior to the
    back pressure doors that have been employed in Germany which minimize
    the amount of cleaning necessary but resulted in cracking of the oven
    walls. The work rules provided in the agreement require constant
    supervision, continuing door maintenance and prompt repair of any
    defective doors. Additional doors and separate alloy steel door seals
    will be kept on hand and refractories for lining doors will be main-
    tained.
    The Company agrees to install and operate a quench car water
    fogging system and prepare and maintain work rules and procedures re—
    lating to the system. This facility will be installed within six
    months from the date of the entry of the Order at an estimated cost
    of $60,000.00. The fogging system is an interim operation and
    will be subject to review by the Board as set forth below. The
    evidence received at our recent hearings on control of air contaminant
    emissions CR 71-23) indicates that enclosed systems for control
    of emissions from pushi~ng are commercially available. The regulation
    requires their installation by December 31, 1974 (Rule 203(d) (6)
    (B) (ii) (bb)). See opinion in the matter of emission standards,
    R 71-23, April 13, 1972, p. 24. Abatement equipment to control
    emissions from the pushing of coke is still in the developmental
    stage. Various types of hoods, both stationary and moveable,
    have been under experimentation in Germany, Japan and to some extent,
    in the United States CR. 3588—3635), Some metallurgical and wind
    problems have developed which must be resolved in the use of this
    facility. Also weight of the unit has created problems when attached
    to a moving charge car. The fogging system to be employed by the
    Company pursuant to the agreement is considered to be the best interim
    method for minimizing emissions from the pushing operation pending the
    improvement in the technology and reexamination by the Board. The
    system to be employed is similar to that used by the Zoliverein Coke
    Plant in Essen (R. 3632—3635). Water is sprayed out of two sides of the
    quenching ear onto the coke. The unit is considered to have a 50
    efficiency and is considered more effective than the hood particularly
    since the system remains in operation during the movement of the car
    from the pushing position to the quench station. The fogging system
    is proposed as an interim method pending improved technology in this
    field. Paragraph 6 of the
    agreement, page 11, provides as follows:
    “At the end of twelve and twenty-four months from
    the
    date of an Order of the Pollution Control Board
    approving this Stipulation, the Environmental Protection
    Agency shall, in consultation with Granite City Steel
    Company, evaluate (1) the effectiveness of the Water
    Fogging System, and (2) the state of technology of control
    of emissions from pushing of coke from coke ovens~ The
    evaluation shall include a specific determination of the
    reasonableness
    of any alternative method of control, if
    4 —
    460

    any, based on the state of technology, econoi~ic
    reasonableness and the emissions to be controlled.-
    If at the end of either twelve month period, the
    Environmental Protection Agency shall determine that
    the Fogging System is not as effective a control of
    pushing the coke from coke ovens as an alternative
    system or systems, based on the state of technology,
    economic reasonableness, and the emissions to be con-
    trolled, then the Environmental Protection Agency shall
    inform Granite City Steel Company and shall report to the
    Pollution Control Board the system or alternative systems
    which it determines should be installed and suggest a
    reasonable time schedule for installation. Determinations
    and evaluations of the Environmental Protection Agency
    may be submitted to the Pollution Control Board by either
    party for review and appropriate orders at the end of
    twelve or twenty-four months.
    During said twelve month periods, the Environmental Pro-
    tection Agency and Granite City Steel Company shall inform
    each other of improvement-s in the state of technology and
    may request discussions and exchange of information related
    to said improvements in the state of technology.”
    It will be seen from the foregoing that the Board reserves jurisdiction
    for such further orders as are appropriate in consideration of alter-
    native systems which may develop over the next two-year period. Exhi-
    bit 87 in the record is a review of the state of the art on control
    of emissions from pushing coke, reviewing the various methods under
    experimentation including forms of hoods and continuous movement de-
    vices being developed throughout the world.
    The Company agrees to install a quenching station baffle system
    within six months from the date of the entry of the Order at an esti-
    mated cost of $130,000.00 which again is represented to be the most ad-
    vanced state of the arts for this particular facility. Two systems
    have been used to abate emissions during the quenching operation. These
    have been the use of water jets and the use of baffles (R.35l0—35l2).
    The baffle system is considered a better form of emission control. The
    quenching tower designed for Granite City Steel Company is divided into
    three parts. A baffle consisting of wooden bars will be built into each
    part. Steam produced during the quenching will be unable to emit direct-
    ly into the atmosphere but will be changed in direction by the bars in
    the baffle. As the dust-laden steam hits the baffles, the dust is re-
    moved from the steam. Water jets are installed to force soot downward,
    which is then flushed away into a settling basin.
    The Company has already installed a smokeless excess blast fur-
    nace gas bleeder burner stack at an approximate cost of $35,000,which pre-
    vents the emission of carbon monoxide built up in the blast furnace from
    entering the atmosphere and assures its burning without creating smoke
    in the process.
    4
    —461

    With respect to the sinter operation, the Company will in--
    stall a Venturi Scrubber System on the Main Windbox, within 19-1/2
    months from the date of the Order at a cost of $1,200,000 designed to
    meet specified process weight rate values and in the alternative,
    if the operation cannot be controlled to meet the standards set forth,
    the sinter operation will be suspended until the standards specified
    are met. Control of the Main Windbox emissions as proposed will
    meet the recently adopted particulate emission standards for this
    facility (Sec.203(a) and 203(d) (2)).
    The Company further agrees to install and operate a bag house
    cleaner on the sinter breaker process to be installed within sixty
    days from the later of the date of theentry of the order or the date
    the sinter process is next operated after the entry of the Order.
    This will likewise bring the breaker process into compliance with the
    new particulate regulation 203(a).
    Surety bonds, each in the amount of the installation cost of
    each facility, respectively, in accordance with the terms of the
    agreement and payable on forfeiture to the Environmental Protection
    Agency are to be furnished, guaranteeing installation and performance
    of all of the facilities above provided. Forfeiture shall take place
    upon non—compliance with the terms of the agreement. The forms of
    bonds are incorporated in the stipulation and order of the Board.
    Provision is made for inspection of all of the eouiprnent and
    installations covered by the agreement. Compliance with particulate
    regulations shall be determined by procedures described in ASNE Power
    Test Code 27-1957 and results submitted to the Environmental Protection
    Agency.
    The AISI Coke Oven Air Quality Control System shall be operated
    at the best attainable effectiveness using the best available technology
    and methods within its basic design capabilities as fabricated and
    installed in accordance with basic design drawings within 30 months.
    Determination of whether such operation does, in fact, meet these stan-
    dards shall be determined in a proceeding before the Pollution Control
    Board. Provision is made in the Stipulation and Order for
    the
    author-
    ization for inspection and investigation by the Agency and notification
    to the Company. The Company, during the entire period of the Agreement,
    shall continue a research and development program evaluating existing
    in-house pollution control equipment, investigate new technology and pro-
    cesses and program the installation of improved control equipment to
    comply with higher emission standards as required by law.
    The Agreement further provides that during the time specified
    for the completion of the program, for each named facility,
    no enforcement
    action shall be brought pursuant to Sections 31(a) and Cc) of the
    Environmental Protection Act for particulate air contaminant emissions
    beyond the limitations of the regulation applied to each facility, pro-
    viding a variance of the Board or bond is then in effect.
    4 —
    462

    Variances are provided for the following operations for
    the periods indicated:
    Coke oven operation, including transporting coke to quench
    tower (except charging) for twelve months;
    Quenching operations
    six months;
    Sinter breaker process stack
    -
    60 days from the date
    of the Order or date of operation after Order, whichever
    is later;
    Charging and any operation of which charging is considered
    a part
    -
    one year, with completion anticipated in thirty
    months;
    Sinter process
    main windbox
    one year, with completion
    anticipated in 19-1/2 months.
    The Company shall make application to the Board for desired extensions
    of variance beyond the original one—year allowance.
    If the Company shows satisfactory progress to the Agency, ex-
    tension of the variance shall be recommended by the Agency to the
    Board. For purposes of extending variance “satisfactory progress” as
    used in the Environme,ntal Protection Act shall be substantial compliance
    with the program of installation as set forth in the Stipulation.
    Attached to the Stipulation as an exhibit is the proposed compliance
    program for each facility, respectively, together with work rules and
    operational procedures to be employed to assure compliance with all
    provisions of the Order.
    In addition to the above facilities covered by variation with
    respect to which specific installations are to be made, work rDles
    and operational procedures are embodied in the agreement for the basic
    oxygen furnace, the blooming mill, the hot strip mill and the steam
    generating facility for which no new installations are provided nor
    variances granted. Procedures to be employed in the event of upset
    and breakdown are included and details as to research development and
    reports are provided. Expenditures totaling in excess of $4,000,000
    will be made for installation of equipment to implement the abatement
    program and should be completed within thirty months from the date
    hereof.
    The testimony of witnesses for the Environmental Protection
    Agency and the Company support the view that the proposed installations
    represent the most advanced state of the arts for abatement equipment
    and control of particulate emissions for each facility involved. Coxm-
    parison between the specifics of emission control
    to be achieved by
    the equipment to be installed compared with the regulations for air
    4 —
    463

    contaminant emissions recently adopted by the Board sustains the view
    that the Granite City Steel Company will be in compliance with the new
    regulations upon completion of contemplated installation program, ai-
    though by reason of the variances allowed and anticipated, the dates
    of actual compliance may, in some instances, go beyond those expressly
    specified in the regulations. The testimony of Dr. Werner Eisenhut
    (R. pp. 3416—3912) supporiE the view that the installations proposed
    with respect to the coking operation and specifically, as to the
    charging by the AISI Larry car, the fogging mechanism to be employed
    during pushing, and the baffle system to be installed in the tower for
    quenching, represent the most advanced abatement facilities in the world
    at the present time.
    Substantial testimony at the earlier hearings related to alter-
    native means both employed e~nd under consideration to control emissions
    from these operations,
    nuns.
    of which appears to assure abatement in.~amore
    suitable form than those which are to be installed by the Company pur-
    suant to this Agreement.
    The Venturi Scrub1~eron the sinter process Main windbox and the
    bag house to be employed in the sinter breaker process again represent
    the best technology to achieve abatement from these sources. These
    views were confirmed by Adolph Biss, Metallurgical Specialist employed
    by the Division of Air Pollution, Illinois Environmental Protection
    Agency (R. April 12, 1972, page 85).
    Dr. John Roberts, manager of the Air Pollution Control Division
    of the Illinois Environmental Protection Agency testified as follows:
    (R. April 12, 1972, p. 81)
    “The improvement in air quality as a consequence of
    Granite City’s proposed program is expected to be sub-
    stantial. According to the Agency’s calculations, com-
    paring total emissions of particulate matter from the
    Granite City Steel facilities immediately prior to the
    filing of this suit in November of 1970 with emissions
    of particulate matter which are expected following com-
    pletion of the proposed control program by the end of
    1974, and assuming good housekeeping procedures,, particulate
    emission can be estimated to decrease by over 90. In
    terms of improvements in air quality in the Granite City
    area, this reduction in particulate emissions should lead
    to a corresponding reduction of approximately 90 micrograms
    per cubic meter in the annual geometric mean concentrations.
    What this means to the citizen of Granite City is that the
    average amount of particulate matter in the air will, after com-
    pletion of this program, be cut approximately in half. In
    terms of health benefits to the citizen of Granite City
    this control program coupled with controls to be effected
    by other industries in the Granite City area as a consequence
    4
    464

    of their compliance with applicable air pollution con-
    trol regulations, will reduce air pollution levels to
    a safe margin below the national health—related standard.
    In terms of economic benefits, I can cite a study by
    I. Michelson and B. Tourin, ‘Comparative Method for
    Studying Cost of Air Pollution.’ Public Health Report.
    Vol. 81(6), pp. 505-511, June, 1966 concerning Upper.
    Ohio River Valley in which a comparative analysis of annual
    per capita cleaning costs incurred in two cities (Steuben—
    ville with particulate levels comparable to those in
    Granite City in 1970 and Uniontown comparable but higher
    than those to be attained by 1975 in Granite City) showed
    a cost saving of $84.00 per capita per year.”
    At the last public hearing in Granite City on the proposed agree-
    ment, some testimony was received regarding alleged excessive emissions
    from the stack of the basic oxygen furnace. No variation is sought
    for these facilities
    nor is any new abatement equipment required to
    be installed pursuant to the agreement and order. Electrostatic pre—
    cipitators have been previously installed on the basic oxygen furnace
    and both the Agency and the Company represent that this equipment,
    plus the work rules, to be enforced, will assure compliance from this
    source. However, if such does not prove to be the case, the Agency is
    in no way foreclosed from taking such action as is appropriate to assure
    that this portion of the operation be brought into compliance if, in
    fact, it is not presently complying.
    In the
    record are several statements from government officials,
    both state and municipal, and Southern Illinois University professors
    questioning whether the University of Illinois at Champaign is the
    appropriate recipient of the scholarship fund provided in the stipula-
    tion. The view expressed by these persons is that since the Metro—East
    Region has been the principal victim of
    the Company’s past emissions,
    the money should be expended in the area affected and more particularly,
    at Southern Illinois
    University.
    While we are not without sympathy
    to this expression of attitude, we are satisfied that the University
    of Illinois,
    with its medical, engineering and law schools, in addition
    to its basic Liberal Arts and Science Programs is a suitable entity to
    carry out the
    objectives of the grant, particularly since the parties
    have agreed to this program as part of the overall settlement of the
    case ,and we are not disposed to alter this provision.
    The agreement in the present case is a milestone in pollution
    control and all parties involved are to be commended.
    It represents
    what is capable of achievement by cooperation between industry and the
    State and furnishes a solution which is both technically feasible and
    economically reasonable, to the benefit of the immediate community,
    the Company itself and the people of the State of Illinois.
    I, Christan Moffett, Clerk of the Illinois
    Pollution ~trol
    Board,
    certify that the above Opinion was adopted on this
    3
    day of May,
    1972, by a vote ~
    4
    465

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