1. 10—333

ILLINOIS POLLUTION CONTROL BOARD
December 13, 1973
GOODYEAR TIRE AND RUBBER CONPANY,
(North Chicago plant)
Petitioner,
v.
)
PCB 73—339
ENVIRONMENTAL PROTECTION AGENCY,
Respondent.
Richard R. Wilfong, Attorney for Petitioner
Lee A. Campbell, Assistant Attorney General for the EPA
OPINION AND ORDER OF THE BOARD (by Mr. Henss)
Goodyear Tire and Rubber Company filed a Petition requesting
variance from Rule 408(a) (lead) of the Water Pollution Control
Regulations of Illinois. Petitioner is engaged in the manufacture
of wire and textile reinforced rubber hose at its North Chicago plant.
The plant employs about 700 persons, operates 24 hours per day, 7
days per week and produces about 300,000 ft. each day of automotive,
industrial and hydraulic hoses.
Part of the operation is the forming of rubber and wire or
yarn into various types of hose and curing it into a finished
product. The curing process involves use of a lead sheath which
serves as a temporary mold for the hose. The hose, encased in lead,
is placed in a heater where temperatures of from 300°F. to 310°F.
are maintained for 30 to 60 minutes in order to vulcanize or cure
the hose. Heat for this vulcanizing process is supplied by steam.
After the vulcanization has been completed, the lead sheath is
cooled by spraying water from high velocity nozzles for a period
of from 8 to 12 minutes. Lead oxide formed on the outer surface
of the lead sheath is dislodged from the sheath during the cooling
period and is carried away in a solid form in the waste cooling
water. The lead sheath is then removed and melted for reuse.
Petitioner uses the vulcanizing process about 40 times per day
which requires an average of 400,000 gallons of well water per day
10—333

for cooling. The water is used on a once through basis and is
then discharged into a treatment facility which serves primarily
as an oil-water separation basin. Approximately 1.2 MGD of
effluent are discharged through the plant outfall to the Skokie
Drainage Ditch, tributary to the Skokie River. Petitioner’s
outfall normal1~ serves as
the
“head ~aters” oi
the
Sko1~c.~eDitch
(R. 76). Flow in the ditch near the point of discharge has a
7-day, 10 year low flow value of 0.84 MGD.
Rule 408(a) limits Petitioner after December 31, 1973 to a
lead concentration in the effluent of 0.1 mg/i (or about 100 ppb).
Monthly operation reports submitted by Petitioner to the Agency
for the first 9 months of 1973 show that lead concentration in 24
hour composite samples were as follows:
MONTHLY OPERATION REPORTS-- INDUSTRIAL EFFLUENT
Lead cppb~
Month
Average
Jan/73
260
Feb/73
270
Mar/73
350
Apr/73
240
May/73
100
Jun/73
100
Jul/73
220
Aug/73
250
Sep/73
233
Goodyear stated that all constituents in the plant effluent
were within regulatory standards except for BOD and lead. The
variance request did not apply to the excessive BOD concentration
since Petitioner plans to connect the plant sanitary system to the
North Shore Sanitary District system in the near future.
Recognizing the problem caused by the excessive lead discharge,
Petitioner engaged the Nalco Chemical Company to conduct a process
waste water study. This study was to determine the source of the
2 lbs./clay lead discharge and the most effective means to reduce
the concentration to meet the Standard. Upon determining that
the lead oxide from the sheath is the source of the. lead discharc~e,
Nalco recommended installation of a special filtering system to
handle the water waste from the vulcanizing process. Total cost
for the system was estimated to be $189,530.
Goodyear accepted the Nalco recommendation and received
corporate approval for inclusion of the project cost in the plant
budget. Goodyear
then
submitted its Project Completion Schedule
to the Agency stating that compliance would be achieved through
the use of the filter system by December 31, 1973. The Agency
approved the Project Completion Schedule on June 28, 1973.
10
334

—3—
For some time before completing its Project Completion Schedule,
Goodyear had an intensive research project underway to determine
if
the process requirement for the lead sheath could be eliminated.
At
several of its other hose plants, Goodyear had developed a new
curing method called the
“open
steam” process. Success at
the
other plans was
in
part
due to the less critical
tolerance
on
dimensions and physical
properties required of the hose produced
at these plants. In addition to providing a more economical
method of producing hose, the steam process completely eliminated
the requirements for lead sheathing thereby eliminating any lead
in the plant effluent.
Hose produced at the North Chicago plant was required to meet
more demanding tolerances than hose from the other plants because
of the critical service under which it would~have to perform.
In early 1973, Petitioner claims a major breakthrough was achieved
for the North Chicago plant. It was discovered that cosmetic type
blemishes and flat spots which developed in the hose during the
vulcanizing process could be effectively controlled by corrugating
the hose prior to vulcanization. Trials using the new technology
began at the plant in early 1973 and, after internal testing had
convinced corporate officials that the project was successful,
samples were sent out for customer approval.
Goodyear now proposes to abandon the waste water filter system
in favor of conver.ting a significant portion of the vulcanizing
process
to the open steam method. Plant Manager Jerome F. Wolf
estimated that ii to 20 of the conversion had already been.
achieved (F. 36) Petitioner has compared data ~for the last six
months of 1972 (before conversion to open steam commenced) with
data for the first six months of 1973 (after conversion commenced)
This comparison allegedly shows a reduction from 269 ppb to 222 ppb
or about 17.5 in the effluent lead concentration. Petitioner
attributes this reduction directly to the conversion to th.e open
steam method of vulcanization.
Based on the reduction thus achieved and on future conversions,
Goodyear estimates that compliance with Rule 408(a~ can be
achieved by Decerr~er31, 1974 with.out need for the
$189,350
filter
system.
After making the decision to convert, the vulcanization process
to the open steam method in lieu of the proposed Nalco filter
system, Petitioner contacted Nalco for information on the effects
of the lead on the receiving stream. Nalco~sProject Manager
Frank J. Pokorny, performed a study which included contact with
university professors, a literature search and personal observations,

—4—
Pokorny testified that as a result of his study, he “arrived
at the conclusion that there is no significant detrimental effect
to the receiving stream from the amount of lead being discharged
from your North Chicago Goodyear hose plant”. (R. 155) It was
his belief that the Skokie Ditch at the point of discharge would
not support higher aquatic forms such as fish (R. 158).
In making this determination, Pokorny testified that he
used a Goodyear study of grab samples taken at various distances
downstream from the plant’s outfall. The grab samples were taken
on September 11, 1973 at the plant outfall, one-fourth mile
downstream from the outfall, one—half mile and one mile downstream.
Analysis of the samples revealed lead concentrations of less than
100 ppb at the outfall, 200 ppb at the one—fourth mile point, and
less than 100 ppb at both the one-half mile and one mile points.
(Ray Warner, Goodyear Manager of Engineering, testified that
the low outfall concentration was probably because the sample was
taken at a time when no hose cooling was taking place. However,
Warner’s conclusion does not conform entirely to other evidence
concerning Petitioner’s waste water treatment system. It is
difficult to understand how the low lead concentration in the
effluent could be directly attributable to Petitioner’s cyclical
water cooling periods since the effluent apparently emanates from
a large holding pond rather than direct and immediate discharge
from the process. While this point is not critical to Petitioner’s
position, the apparent discrepancy should have been explained more
clearly.)
Pokorny also testified that his conclusion was based in part
on information published in the document Water Quality Criteria
by McKee and Wolf. A section of that’ document relating to lead
oxide states “apparently insoluble lead is not toxic to fish”
(R. 160)
The Agency produced no witnesses or evidence to refute
Pokorny’s testimony but did argue the point in its Recommendation.
The Agency said:
“Based on presently available data, the Agency believes
that Petitioner’s allegations concerning the negligible
adverse environmental impact associated with its lead
discharge cannot be conclusively substantiated nor
refuted. Excessive aqueous lead concentrations are
readily dissipated through the sedimentation of
particulate lead and the sedimentary adsorption of
ionic lead species. However, the physiochemical
dynamics of lead transport between the sediment-water
10—
336

—5—
interface are not well defined. Additionally,
there remain many questions surrounding the potential
for sedimentary lead to enter benthic organisms and
ultimately higher levels of the aquatic food web.”
While we find this statement interesting, it fails to refute
the Pokorny testimony in any manner. We shall, therefore, accept
Pokorny’s conclusion for the purpose of this variance only.
The North Chicago plant has experienced earnings deficits
since 1969. Testimony by Petitioner’s manager of accounting
revealed that while the Goodyear Corporation was experiencing
net profits of from 4.7 to 4.9, the North Chicago plant experienced
a net loss based on net sales of 4.5 in 1969, 7.16 in 1970, 7.4
in 1971 and 3.3 in 1972 (R. 120). However, current figures for
1973 show a net profit of about 0.1 (R. 42)’. The accounting
manager indicated that installation of the proposed filter plant
would severely jeopardize the potential net profit the plant
might experience for 1973.
Petitioner’s witnesses unanimously agreed that the degree of
conversion to the open steam method is dependent upon customer
acceptance of the new corrugated hose, but they did not agree on
methods to be employed in the event customer approval is not
obtained. Wolf testified that such an event would force Petitioner
to install the $190,000 filter system even if it could be used for
only one year (R. 55)
.
On the other hand, Warner testified that
the strategy would probably be to select the heaters producing the
most lead discharge and install individual filter systems on those
units (R. 116). From this we conclude that there are several
control methods available, and the testimony is a positive indication
that some method~, either a small or large filter system or conversion
to the open steam method will be in operation by December 31, 1974.
Wolf and Robert H. Feucht, Development Manager were confident that
the proposed schedule for achieving compliance by December 31, 1974
could be bettered, although neither could say how much earlier
compliance would be achieved.
Based on the entire record, it is our opinion that Petitioner
has met the requirements for receiving a variance. Research by
Goodyear has shown that the source of lead in its effluent can be
significantly reduced by a change in process. Where such process
alterations have the capability of producing an acceptable effluent,
the Board will readily endorse the process alterations in lieu of
expensive control equipment. Eliminating lead in the process
rather than through waste water treatment unquestionably embodies
the best form of pollution abatement. To force Petitioner to
install the $190,000 filter system at a time when process changes
10—337

—6—
should achieve compliance within one year would indeed be
arbitrary and unreasonable.
Testimony by Pokorny relating to the environmental effects
of the lead in Petitioner’s effluent stands unrefuted. The
Pokorny testimony, the reductions in lead concentration already
achieved, the commitment to come into compliance during 1974,
all indicate that the economic impact from installing the
$190,000 filter system significantly outweighs the possible
detrimental effects of this effluent on the Skokie Ditch.
The Agency recommended denial of the variance unless
Petitioner could show that 1) continued lead discharges to the
Skokie Ditch would have no significant environmental impact,
and 2) that conversion to the open steam process could not have
been initiated at an earlier date or accelerated to enable
timely compliance with Rule 408(a). It is our opinion that Good-
year has made such proof. The EPA said that, if Petitioner
proved these two points, the variance should be granted subject
to a schedule calling for periodic decreases in the lead con-
centration based on 24—hour composite samples. This schedule
is precisely the same schedule Petitioner proposes to adhere to
(Petitioner Exhibit 1) and we shall grant the variance subject
to the agreed effluent reduction schedule.
ORDER
It is the Order of the Pollution Control Board that:
1. Goodyear Tire and Rubber Company, North Chicago
plant, is granted a variance from Rule 408(a)
of the Water Pollution Control Regulations of
Illinois until December 13, 1974, in order to
make such process alterations or such installation
of control equipment as may be required to achieve
compliance with said Rule.
2. This variance is subject to the following condition:
effluent lead concentrations shall not exceed
the
following monthly average levels based on weekly
24 hour composite samples:
Date
_____
January 1, 1974
0.211
April 1, 1974
0,179
July 1, 1974
0.160
October 1, 1974
0.154
December 1, 1974
0.100

—7—
3. Goodyear Tire and Rubber Company shall, by
January 3, 1974, post a bond in the amount
of $20,000 in a form acceptable to the
Environmental Protection Agency, such bond
to be forfeited in the event Petitioner fails
to make such process alterations or such
installation of control equipment. The bond
shall be mailed to: Fiscal Services Division,
Illinois EPA, 2200 Churchill Road, Springfield,
Illinois 62706.
4. Goodyear Tire and Rubber Company shall provide
the Agency with quarterly progress reports,
commencing January 3, 1974. Such reports shall
completely detail all progress or lack of progress
towards achieving compliance with Rule 408 (a).
I, Christan L. Moffett, Clerk of the Illinois Pollution Control
Board, hereby certify t~eabo~e Opinion and Order was dopted
this /3’~’~ day of ~
1973 by a vote of ____to (~
~4ieeL

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